I fired up my XB to go for a ride for the first time this year.....er I think it was the first time this year (brain fading?) I’m beginning to lose track without flicking back through my diaries.
Last ride WAS to the MOT early last November.
The great thing about EFI is not needing to purge then re-prime carbs for any hope of it firing on today’s E5 fuel. The little XB started immediately on the first prod then settled into the idle.
Taking it gently for the first 10 miles I kept to 50 mph country roads and a self imposed 3000 rpm limit to warm up and evaporate any moisture then gradually edge up towards 3500 or more. RESIST, RESIST gassing it hard I told myself.
I like to reach at least 26 miles plus or minus at which point a waft of hot air is emitted from the rear cylinder head onto my right leg to tell me that the motor is up to temp and cooking steadily!
Imagine my disappointment when I stated to gas it over 4K only to hear more exhaust noise than power as if the muffler had fallen off. It was a bit like one of those old 1338 HDs with badly matched open pipes; all growl and no grunt.
Keeping in medium gears and winding it through the Rev range the gutless feel evaporated and the speed was there, but the explosive surge I used to get from 3800 to 5200 was absent. I thought that maybe my XB12 muffler had corroded during lockdown and a hole had blown out causing a loss of some critical back pressure. This all seemed a bit odd as the barometric air pressure was healthy today. Or maybe the air box temp sender had just taken longer to wake up today!
After some more miles things started to improve and midrange response became more healthy and the noisy ‘bark’ when loading the throttle at lower revs had become more muted. The bike was getting steadily faster. I then started to think that the nearly full tank of fuel I started with which had been standing for over 5 months had ‘gone off’ despite me adding a measure of fuel stabiliser. That must be the reason as the motor had not missed a beat all day and seemed to be fuelling cleanly. Only time to cover 88 miles in total today so I’ll just have to run the fuel through with a second run before I can refresh the tank with new 99 RON.
Apart from these gripes everything else on my 9 worked well, no oil leaks, no electrical gremlins. Even the typically flakey neutral light worked when it was supposed to.
Hope yours works too!